Monday, June 27, 2011

C-4 Galley, Signed, Sealed & Delivered.

Here’s a cool photo taken by Abra. Thanks to John Finch of Colorado for suppling the galley and slide. Abra delivered the galley to the museum in person, and it now lives with this handsome C-4 Intertype at the East Iceland Technical Museum. Sounds like a fun adventure. I didn’t think to ask Abra about the keyboard layout. I believe letters such as the “eth” and “thorn” are unique to the Icelandic alphabet, how would these letters be arranged / positioned? Also, which typefaces would have been supplied with these letters? Hmmph. Well, seems like a trip to Iceland is in order…

Friday, May 6, 2011

Wanted: C4 galley

Abra Ancliffe, local letterpress printer and Pacific Northwest College of Art instructor is looking for an Intertype C4 galley for her friends at the Technical Museum of East Iceland in Sedisfjordur, Iceland.

I believe that the machine is in working order, or close to it. Abra is hoping to track down a galley before she visits Iceland next month so that she can deliver it to the museum.

If anyone has a galley that will fit, please let me know. Otherwise, we may be able to dig up another galley in the Portland area. If someone can let me know if galleys for other models are interchangeable with the C4, and/or if a Linotype galley can be easily adapted to fit I’d appreciate the info.

Here are some photos that Abra forwarded of the galley-less Intertype in Iceland:






Monday, April 4, 2011

Keyboard Cam Roller Friction Spring.

Here’s a simple fix that made a big difference. The slightest amount of resistance caused the keyboard rollers to stop. Even the normal action of depressing a key could cause drag, and it was necessary to give the rubber roll shaft gear a bit of a push to keep things rolling.


After tapping out the collar pin, I gave the friction spring and shaft pulley a splash of white gas and a good scrubbing. Then I carefully bent the spring to give it a bit more tension against the pulley. Much better.

Short Keyboard Rods

Pictured here is the keyboard swung open with the keyboard cam yoke frames removed and various keyboard shields removed. It is important to make sure that no key rods are engaged before the keyboard is swiveled into this position.  If a short keyboard rod is raised when the keyboard is rotated, it *will* bend and it will cause problems. This keyboard had been opened in this manner, and was in need of repair. When swinging out the keyboard, It seems like it is really easy to overlook this detail, especially when all of the shields are in place. I suppose it’s one those things that you learns as Linotype operator: you make the mistake once and you probably won’t do it again. It was a simple fix, but like anything else on this machine it took a little patience and some time.
Here’s a view of the backside of the keyboard. On this machine, the keybars can be removed as a unit. However, the lower key rods cannot.
Sign of trouble. After running my finger along the bottom of the short keyboard rods, most fell back into place as they should. These stuck.
Removing the short keyboard rods was a bit fussy. As soon as I loosened the guide bar, the rods wanted to fall through. Could have been a big mess. It was my goal to keep them in the proper order. If anyone has a trick for this, please let me know. I ended up hand scoring a piece of 18pt board to the dimensions of the bars, and cupped it around the bottom while removing the rod guide. This kept the rods in position so I could clean and straighten them in order.    
Here you can spot the bent rods. If you look closely, you may also be able to see that the brass guides that space the bars have also been damaged. Some are pinching the rods so they cannot move freely. Here I took a small flat-blade screw driver and very gently tapped them back into place. Apparently, I was lucky. Bill Spurling told me that he has seen machines with paper clips or little pieces of wire that replace the brass teeth that have been broken off. This one was in relatively good shape.
Here is a profile view of a bent rod. I used a mallet to straighten it.
More cleaning. Wow. These were really gummed up. But with straightened guides and straightened rods and a bath of white gas, they were as good as new.

Tuesday, March 29, 2011

Bill Spurling & Linotype.org

Brian Donnell seated. Bill Spurling standing.
At Bill Spurling’s Place. 
Bill Spurling is a great resource for linotype operators and enthusiasts in this region and beyond. He and his son Tristan have managed to save many machines from the scrap yard including these:

1912 Model 5, 1922 Model 8, 1923 Model 8, 1924 Model 14, 1938 Model 29, 1946 Model 31, 1949 Model 31, 1949 Model 30, 1962 Model 30, 1960 Model 29

Many of the above listed machines have been stripped down and rebuilt by Bill, so it’s been great to pick his brain while learning tricks and general maintenance on our 31. He has been generous with his time and spare parts when needed. Also, one of his 31s is a cousin of our machine. It shipped in the same year and is only 302 machines younger than ours, so it has been helpful to study a nice clean runner for comparison.

Bill is the man behind the website Linotype.org which is full of useful information including a chart of machine serial numbers, downloadable .pdf manuals, regional linotype history, etc. From his site: “This site is dedicated to the unsung heros that made it all work, the Linotype Machinists and Machinist-Operators everywhere, past, present and future.” Hear, hear.

Monday, March 28, 2011

Brian Donnell

Brian Donnell operating a 6 pocket, “2 in 1” Linotype 31
at Advanced Letterpress in Portland, Oregon
Brian Donnell has bailed me out on several occasions when I’ve found myself in over my head with linotype issues. When he doesn’t have the answer, he will offer what I like to call a “Donnellism,” which is a story or a bit of wisdom that somehow relates to the problem. This tidbit always leads me to finding a solution to the problem, even if it hits me hours later. Brian is a good teacher that way. As a journeyman printer, Brian is one of the young “old guys” who in 1974 got his start at the end of an era that was at the height of printing craftsmanship. Brian is generous in sharing his knowledge, and has created an excellent on-line primer for letterpress printing. Check it out here. Also, Brian can be found on Briar Press here. 

Wednesday, March 16, 2011

Replace Keyboard Rubber

Many of the keys had a very slow response, or no response at all which is often due to old glazed & hardened rubber. The idea is that the surface of the hardened rubber doesn't provide enough friction for the cam to rotate, so it wobbles and skids along the surface until it catches. Also, it is not uncommon for the key cams to be over oiled causing oil to drip onto the surface of the rubber roller and breaking it down prematurely.

Bill Spurling mentioned that he has seen rollers that appear almost as if they have been sliced by the cams. The roller I was mostly concerned about wasn't that bad, but it was glazed quite a bit, and it did have some pretty good grooves worn into the surface.

As you can see from the photo below, oil also creeps in through the oil points at the ends of the frame. Good thing to remember to not over oil these.

Here you can see that the rubber has broken down and filled the space in between the teeth creating a smooth surface across the cam.
I've heard that replacing the rubber can be a bit of a challenge. It's pretty tricky to slide the thick walled rubber roll onto the steel core. Apparently there is a tool for this job, and apparently folks like Dave Seat make this process look as easy as the book describes. The book will describe the steps: “slide the rubber on while holding your thumb over the end. This will cause the air inside to be compressed and cause the roll to expand and slip easily upon the shaft.” Really? Sounds like a snap. But, honestly, I knew I was looking at a project. Brian Donnell had also told me that he had spent a lot of time fighting with the keyboard rubber years ago when it was necessary to replace his.

I tried to apply a bit of rubber rejuvenator, a product that we keep around the shop for use when the offset dampening rollers become glazed. It did seem to bring back a bit of life to the rubber. The surface of the rubber roll had a little less sheen. But after studying the caked cam teeth once more, and perhaps because I can be a bit of a glutton for punishment, I decided to replace the rubber.


No turning back now. Of course the books say: “slip the old rubber off” or something like that. There was no slipping. The rubber roll liked the steel core and wasn't planning on going anywhere. The book the mentions: “it may be necessary to slit the rubber length wise to remove it.” Yup.
After removing the old rubber roll, I inspected the core. It was a bit like inspecting the growth rings on a tree stump. I could count at least 5 faint knife score lines produced by the hands of operators and mechanics from the past. A bit humbling. It was kind of cool to be the 6th score line on the core.
Now the fun. Apparently by swiftly whacking this rubber roll on to the core, the seal of one’s palm will be enough to push air through, expanding the almost 1/4 inch thick rubber roll easily into place. I managed to get about 1/16th of the way on. I struggled with this for about 30 minutes. I found a tapered steel “plug” to place on the open end, and by pulling and pounding with a mallet, managed to move it on another 1/2 inch.
I decided to employ a second method: “If no special tool is available, the roll may be put on easily by starting one end on the shaft and filling the roll with water. Hold the hand over the top and press down allowing the water to escape as the roll goes into place” I tried this method for another 30 minutes with a little more success. The roll was now 1/3 of the way in place. It was a tiring process. My hands were throbbing and I now had water covering the front of my shirt and pants. Picture this: middle aged man rolling around on the floor with a steel rod and rubber roll, red in the face, cursing and grunting, splashing water over himself. What I didn't realize was that our normally quiet after hours industrial warehouse district was in fact swarming with kids going to a neighboring rave. So what I thought was an empty pitch black quiet side street outside our oversized shop windows was actually filled with young party goers who were probably enjoying the spectacle. Ha! Anyway it was around this time when the magical sweet spot happened. Somewhere around the halfway point, the roll gained momentum, and with a sloppy “swack” it slid into place.

My heart sunk a bit when I discovered this. What?!? The roll is too short? Crap! I didn't measure the roll before I spent the last hour and half fighting with it to go on. After a bit of kneading to rubber into place, the roll expanded. Of course! I just spent all of that time putting pressure on it, no wonder it would compress. Whew.
Here it is, as it should look.
Ready to be placed back into the key cam frame.


Reassembling the frame.



Completed frame, and tired dude.